Loading...
2020.06.25_COD_FollowUp i_ Gas Well Inspection Type 2020 Annual Y Inspections Inspection Cycle 1st Half _ DENTON 24hr Phone g g Inspection Date 5-22-20 855-820-6008 Well Operator Ea lerid e Record Close Date 6-24-20 Active Padsite Name 117 ACME BRICK"C" 1 Jurisdiction CoD Re-Inspection Date 6-24-20 Site Address 163 N. 135 Padsite Type Single Well Rt 57 2nd Re-Inspection Date Ordinance Reg 2002-040 R Weatherby Inspected by y Inspection Status Closed Plat/Site Permit No Plan No Lease Name .RRC Id Aoi No. Spud Date Impact 1108-0057 GWP02-0013 ACME BRICK"C" 1 204270 12132346 8/11/2004 Moderate INSPECTION CHECK LIST Signs/Labels General Location Facility Equipment Operator • Good Need Resolve Wellhead Paint • Good Need Resolve p Fencing • Good Need Resolve Site Address • Good Need Resolve Wellhead Leaks Good Need • Resolve Well Name • Good Need Resolves Entry Gate • Good Need Resolve Site • Good Need Resolve T Battery Paint • Good Need Resolve 24hr. Phone • Good Need Resolves Stains • Good Need Resolve T Battery Leaks • Good Need Resolve RRC/A i# • Good Need Resolve Tank Integrity • Good Need Resolve p� Trash/Debris • Good Need Resolve Containment • Good Need Resolve No Smoking • Good Need Resolves Weeds/Brus Good Need • Resolve Reflective • Good Need Resolves Oders/Fumes/Dus • Good Need Resolve Drip Pots • Good Need Resolve Wellhead • Good Need Resolves Site Lighting • Good Need Resolve Lightning • Good Need Resolve • Good Need Resolve Equip Height • Good Need Resolve Tank Battery Landscaping • Good Need Resolve Tank Labels • Good Need Resolves Erosion • Good Need Resolve No Wells Approved Db Level Miscellaneous Electric Lines • Good Need Resolve Pipeline • Good Need Resolves Layout • Good Need Resolves Markers per Site Inspection Comments Entrance sign needs to be re-posted. Weed control needed. Regulator at wellhead venting needs repair(red flag). Flowline from wellhead to Separator has heavy corrosion. Corroded portion of flowline needs to be replaced or disconnected from Separator. This is a H-15 well shutin on 6/1/18. On 6-24-20,AP conducted a follow-up inspection of the well site with Jeff Smith attending. Operator resolved all issues requiring further attention. Corroded pipe was properly disconnected from separator. Inspections Conducted by Third Party and COD Follow Up Third Party Inspection Date: 4-7-20 COD Follow Up Date: 5-22-20 Corrosion: separator Regarding corrosion,see piping, AST A, and AST m Inspection comments piping A A A, : Loom: wa s.P..,ec. OAST QAnd Wry E P Po N • F.Lori • � Ugnnd An$emphq Ppnl =� '® D-4 A.Sa pwV Pp,l f—.6—Su ng AJ g,--v -- Ob_ry _PatA ® p Pawn.