2018.02.22_COD_Inspection Gas Well Inspection Type 2017 Annual
�oF I n s p e ct i o n s Inspection Cycle 2nd Half
_ DENTOR
24hr Phone 817-588-0372 Well Operator Enervest Inspection Date 12-1-17
Record Close Date 12-28-17
Active Padsite Name 4 Little Brook Estate A#1 1
Jurisdiction CoD Lnc Re-Inspection Date 12-28-17
Site Address 2530 Lovers Ln.
Padsite Type Single Well Rt 08 2nd Follow-up Inspection
Ordinance Reg 2002-040
Inspected by Rod Weatherby Inspection Status Closed
Plat/Site
Permit No Plan No Lease Name .RRC Id Ali No. Spud Date Imoact
1109-0303 No Record Little Brook Estate A#1 1 191382 12131344 5/23/2002 2 High
INSPECTION CHECK LIST
Signs General Location
Operator Name x Good Need Resolved Fencing x Good Need Resolved
Site Address x Good Need Resolved Entry Gate Locked x Good Need Resolved
Well Name x Good Need Resolved
Site Surface x Good Need Resolved
24hr. Phone No x Good Need Resolved
Stains x Good Need Resolved
RRC&Api No x Good Need Resolved Trash/Debris x Good Need Resolved
No Smoking x Good Need Resolved
Weeds/Brush Good Need x Resolved
Reflective/Lighting x Good Need Resolved
Oders/Fumes/Dust x Good Need Resolved
Site Lighting x Good Need Resolved
Facility Equipment I Landscaping x Good Need Resolved
Wellhead Paint x Good Need Resolved
Wellhead Leaks x Good Need Resolved Miscellaneous
Tank Battery Paint x Good Need Resolved Electric Lines Safe x Good Need Resolved
Tank Battery Leaks Good Need x Resolved Pipeline Markers x Good Need Resolved
Equip Height x Good Need Resolved
Layout per Site Plan x Good Need Resolved No Wells Approved Db Level @Inspection
Erosion Control Referred
Fire Dept. I
Fire Lane Access Referred Tank Integrity Referred Foam Lines Referred
Auto Safety Valve Referred Containment Integrity Referred Lightning Arresting Referred
Tank Level Activated Referred Drip Pots @ Disconnects Referred Pit Fencing Referred
Accessible ESD Referred Storage Tank Labels Referred Pit Liner Integrity Referred
Inspection Comments I
DV Controller maint needed, Weed control @ Tank Battery needed. On 12/28/17,RW conducted a follow-up inspection of the well
site.All items requiring further attention from the Operator were resolved.