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2019.01.03_COD_FollowUp i Gas Well Inspection Type 2018 Annual COF I n s p e ct i o n s Inspection Cycle 2nd Half _ DENTOR 24hr Phone 866-535-6836 Well Operator XTO Inspection Date 10-18-18 Record Close Date 12-3-18 Active Padsite Name 5 FITTS 1 Jurisdiction CoD Lnc Re-Inspection Date 12-3-18 Site Address 4234 Masch Branch Rd. Padsite Type Single Well Rt 01 2nd Follow-up Inspection Ordinance Reg 2005-223 Rod Weatherby Inspected by y Inspection Status Closed Plat/Site Permit No Plan No Lease Name _RRC Id Ali No. Spud Date Imoact 1109-0299 GWP06-0010 FITTS 1 30805 12132973 10/12/2006 Moderate INSPECTION CHECK LIST Signs/Labels General Location Operator Name • Good Need Resolved Fencing • Good Need Resolved Site Address • Good Need Resolved Entry Gate Locked • Good Need Resolved Well Name • Good Need Resolved Site Surface • Good Need Resolved 24hr.Phone No • Good Need Resolved Stains • Good Need Resolved RRC&Api No • Good Need Resolved Trash/Debris • Good Need Resolved No Smoking • Good Need Resolved Weeds/Brush • Good Need Resolved Reflective/Lighting • Good Need Resolved Oders/Fumes/Dust • Good Need Resolved Wellhead Sign • Good Need Resolved Site Lighting • Good Need Resolved Tank Battery Sign • Good Need Resolved Landscaping • Good Need Resolved Storage Tank Labels • Good Need Resolved Erosion Control • Good Need Resolved Facility Equipment Miscellaneous Wellhead Paint • Good Need Resolved Electric Lines Safe • Good Need Resolved Wellhead Leaks Good Need • Resolved Pipeline Markers • Good Need Resolved Tank Battery Paint • Good Need Resolved Layout per Site Plan • Good Need Resolved Tank Battery Leaks • Good Need Resolved Tank Integrity • Good Need Resolved No Wells Approved Db Level @ Inspection Containment Integrity • Good Need Resolved Fire Dept. I Drip Pots@ Load • Good Need Resolved Lightning Arresting • Good Need Resolved Fire Lane Access Referred Tank Level Activated Referred Equip Height • Good Need Resolved Foam Lines Referred Pit Fencing Referred Accessible ESD Referred Auto Safety Valve Referred Inspection Comments Wellhead UMV leaking at stem packing needs repair. On 12/3/18, RW conducted a follow-up inspection of the well site.Operator resolved all items requiring further attention.