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2020.06.22_COD_FollowUp _.,./ Gas Well Inspection Type 2020 Annual Cp , Inspections Inspection Cycle 1 st Half _ DENTON 24hr Phone 855-820-6008 Well Operator Eagleridge Inspection Date 5-20-20 Record Close Date 6-19-20 Active Padsite Name 107 Bonnie Brae Pad Jurisdiction CoD Re-Inspection Date 6-19-20 Site Address 3696 S. Bonnie Brae Padsite Type Multi Well Rt 42 2nd Re-Inspection Date Ordinance Reg 2013-014 R Weatherby Inspected by y Inspection Status Closed Plat/Site 'ermit No Plan No Lease Name . RRC Id Api No. Spud Date Impact 1312-0043 Bonnie Brae 2H 276941 12134424 10/9/2013 Moderate 1108-0605 GWP02-0002 BONNIE BRAE 3H 191993 12131597 7/29/2002 Moderate INSPECTION CHECK LIST Signs/Labels General Location Facility Equipment Operator • Good Need Resolve Wellhead Paint Good Need • Resolve p Fencing • Good Need Resolve Site Address • Good Need Resolve Wellhead Leaks • Good Need Resolve Entry Gate • Good Need Resolve Well Name • Good Need Resolves Site • Good Need Resolve T Battery Paint • Good Need Resolve 24hr. Phone • Good Need Resolves Stains Good Need • Resolve T Battery Leaks • Good Need Resolve RRC/A i# • Good Need Resolve Tank Integrity • Good Need Resolve P Trash/Debris • Good Need Resolve No Smoking • Good Need Resolves Weeds/Brush Good Need • Resolve Containment Good Need • Resolve Reflective • Good Need Resolves Oders/Fumes/Dus • Good Need Resolve Drip Pots • Good Need Resolve Wellhead • Good Need Resolves Site Lighting • Good Need Resolve Lightning • Good Need Resolve • Good Need Resolve Equip Height • Good Need Resolve Tank Battery Landscaping • Good Need Resolve Tank Labels • Good Need Resolves Erosion • Good Need Resolve No Wells Approved Db Level Miscellaneous I Electric Lines • Good Need Resolve Pipeline • Good Need Resolves Layout • Good Need Resolve4 Markers per Site Inspection Comments Bare Pipe at wellhead A needs paint, Oil stains around compressor needs remediation. Weed Control needed. Holes in containment needs repair. On 6/5/20, RW&AP conducted a spot inspection. Holes in containment needs repair. All other issues were addressed.On 6/19/20, RW&AP conducted a follow-up inspection of the well site.Operator resolved all items requiring further attention. I Inspections Conducted by Third Party and COD Follow Up I Third Party Inspection Date: 4-7-20 COD Follow Up Date: 5-20-20 Corrosion:separator Issue compliant piping and AST piping ..........�. �y Leaend: ... saP•ra rmw wtir c•.m.n.a �c••v Fa.o..n • • rnm one. C .• • © UpnOAr S•npnq Poti A A • .-i C ® Do..wnE M S P"Punt � � * Wl+a Dn.cem tbl FMM Sn. NIU9rm.nt �•-OC�rv.m PaW I0�