2020.05.26_COD_Inspection _-IM000 Gas Well Inspection Type 2020 Annual
`OF Inspections Inspection Cycle 1st Half
_ DENTOR
24hr Phone Inspection Date 4-23-20
817-841-8885 Well Operator Bedrock
Record Close Date 5-15-20
Active Padsite Name 156 Robson Ranch CTB
Jurisdiction COD Re-Inspection Date 5-15-20
Site Address 12886 Robson Rd.
Padsite Type CTB Rt 21 2nd Re-Inspection Date
Ordinance Reg
Inspected by R Weatherby Inspection Status Closed
Plat/Site
Permit No Plan No Lease Name .RRC Id Ali No. Spud Date Impact
1110-0183 Robson Ranch CTB High
INSPECTION CHECK
Signs/Labels General Location Facility Equipment
Operator • Good Need Resolve Wellhead Paint Good Need Resolve
p Fencing • Good Need Resolve
Site Address • Good Need Resolve Wellhead Leaks Good Need Resolve
Well Name Good Need Resolves Entry Gate • Good Need Resolve Site • Good Need Resolve T Battery Paint • Good Need Resolve
24hr. Phone • Good Need Resolves Stains • Good Need Resolve T Battery Leaks Good Need • Resolve
RRC/A i# • Good Need Resolve Tank Integrity • Good Need Resolve
p� Trash/Debris • Good Need Resolve Containment • Good Need Resolve
No Smoking • Good Need Resolves Weeds/Brus Good Need • Resolve
Reflective • Good Need Resolves Oders/Fumes/Dus • Good Need Resolve Drip Pots • Good Need Resolve
Wellhead Good Need Resolves Site Lighting • Good Need Resolve Lightning • Good Need Resolve
• Good Need Resolve Equip Height • Good Need Resolve
Tank Battery Landscaping • Good Need Resolve
Tank Labels • Good Need Resolves Erosion • Good Need Resolve INO Wells Approved Db Level
Miscellaneous
Electric Lines • Good Need Resolve Pipeline • Good Need Resolves Layout • Good Need Resolves
Markers per Site
IInspection Comments I
@ Compressor 1 - DV controllers venting needs repair(red flagged). @ Compressor 2-DV controllers venting needs repair(red
flagged), Regulator venting needs repair(red flag). Weed control needed. On 4/30/20, RW conducted a follow-up to check venting
issues. Operator addressed the venting issues at the Compressors. Weed Control issue remaining. On 5/15/20, RW conducted a
follow-up inspection of the well site. Operator addressed weed issue.
Inspections Conducted by Third Party and COD Follow Up
Third Party Inspection Date: 3-26-20 COD Follow Up Date: 4-23-20
Leaks:Separator A Reported issues were
actuator,Separator B tested and found working
actuator and kimray valve, properly
AST A enardo valve,AST B
enardo valve,and AST E
enardo valve