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1990-0552651L-9/3689 NO. AN ORDINANCE AUTHORIZING THE EXECUTION OF A CHANGE ORDER TO A CONTRACT BETWEEN THE CITY OF DENTON AND TRI-CON SERVICES, INC.; PROVIDING FOR AN INCREASE IN THE CONTRACT PRICE; AND PROVIDING AN EFFECTIVE DATE. WHEREAS, on October 4, 1989, the City awarded a contract for the construction of certain improvements to Tri-Con Services, Inc. in the amount of $446,797.50; and WHEREAS, the City Manager having recommended to the Council that a change order be authorized to amend such contract with respect to the scope and price and said change order being in compliance with the requirements of Chapter 252 of the Local Government Code; NOW, THEREFORE, BE IT ORDAINED BY THE COUNCIL OF THE CITY OF DENTON: SECTION I. That the change order to the contract between the City and Tri-Con Services, Inc., a copy of which is attached hereto, in the amount of Twelve Thousand Seven Hundred Ninety Nine and 40/100 ($12,799.40) Dollars, is hereby approved and the expenditure of funds therefor is hereby authorized. SECTION II. That this ordinance shall become effective immediately upon it passage andja~roval. ~'~ da of PASSED AND APPROVED this -P y ~~_~ , 1990. ATTEST: IFE~ALTERS, CITY SECR ' APPROVED AS TO LEGAL FORM: DEBRA ADAMI DRAYOVITCH, CITY ATTORNEY DATE: APRIL 3, 1990 CITY COUNCIL REPORT TO: Mayor and Members of the City Council FROM: Lloyd V. Harrell, City Manager SUBJECT: BID# 1007 - MALONE STREET DRAINAGE IMPROVEMENTS CHANGE ORDER #1 RECOMMENDATION: We recommend this Change Order MI be approved in the amount of a $17,199.40 increase. The Contract price will change from $446,797.50 to $463,996.90. SUMMARY: This price increase is due to the unexpected required excavation of rock as per the Contract Terms and Conditions. Also included are several other changes in the project brought on by unforeseen happenings and circumstances. The Memorandum from Rodger McDaniel to Rich Svehla outlines the changes in detail. BACKGROUND: City of Denton Change Order Form, Memorandum dated March 26, 1990. PROGRAMS, DEPARTMENT OR GROUPS AFFECTED: Engineering Department and Drainage Improvements Contractor, Tri-Con Services, Inc. FISCAL IMPACT: Funds for this change will come from the original source of funding #434-002-G088-8808-9108. Res~ct f~t~ y submitted: City Manager Name: Tom D. Shaw, C.P.M. Title: Purchasing Agent Approved Name: Tom D. Shaw, C.P.M. Title: Purchasing Agent 027 .DOC CITY OF DENTON CHANGE ORDER 1. Division (Department)I 2o Purchase Order Noo I 3o Change Order No. Public Works/En~ineerin~ 93185 1 4. Name of Project 5. Project Acct No. 6. Date Prepared Malone Draina§e 434-002-G088-8808-9108 3-23-90 7. Name and Address of Contractor Tri-Con Services, Inc. - P.O. Box 286?? Garland, Texas 75041 8. Description of Work Included in Contract Drainage Improvements for P~lone Street 9. Changes ordered and reason ordered (List individual changes as: A, B, C, D, etc. See attached 10. Bid Original 'Contract Revised Negotiated Original Revised Contract Item Estimated Unit Estimated C.O. Unit Estimated Estimated Changes No. Quantity Price Quantity Price Cost Cost A. B. SEE ATTA HED C. D. Total Total 11. Original Contract Price 446,797°50 Increase in Contract Price 17,199.40 New Contract Price 463~996o90 Decrease in Contract Price 12. Contract time increased/decreased by -8- days. New contract time 50 days THE AFOREMENTIONED CHANGE, AND WORK AFFECTED THEREBY~ IS SUBJECT TO ALL CONTRACT STIPULATIONS AND COVENANTS. S~ection Supervisor Date 14. ACCEPTED BY CITY ENGINEER: Signature Title Date 15. ACCEPTED BY CONTRACTOR: Signature Title Date DIREC~R OF UTIL~TI~: Signature Title Date CONDITIO~ OF APPROVAL: 17o PURCHASING/FINANCE Signature Title Date COUNCIL APPROVAL (If needed) Date CITY of DENTON / 215 E. McKinney / Denton, Texas 76201 MEMORANDUM DATE: March 26, 1990 TO: Rick Svehla, Deputy City Manager FROM: Roger McDaniel, Engineering Tech Supervisor SUBJECT: Malone Drainage Overview Tri-Con Services, Incorporated of Garland, Texas was awarded the contract for Malone Street Drainage Improvements in November 1989. The contract pri~e was $446,797.50. Work began on November 27, 1989. We encountered rock on the project during the week of December 11, 1989. By December 19, 1989, the contractor had excavated 350 cubic yards. The estimated contract quantity for this item was 50 cubic yards at $15.00 a cubic yard. We submitted a memo to the "91" Committee on December 19, projecting between 1200 and 1500 cubic yards as a possible total quantity. The total amount excavated came to 915.6 cubic yards for a total increase of $12,984.00. Considering the existing condition of Gober street along with the additional problem of introducing the heavy equipment needed to complete the storm drain, it became evident that more than the patch over the ditch line would be needed to maintain this streets serviceability after project completion. The contractor was counseled that the asphalt patch would fail due to infiltration of water from the remainder of the street. The existing street was a seal coat over a subgrade of sand and river rock. Tri-Con offered to cement stabilize the entire street from Cordell to Linden at no cost to the City of Denton if the Street Department would do an overlay. James Corbin agreed that this was the best solution because of the potential maintenance problems. He requested that we use the remaining funds for patch to help pay for the asphalt. Tri-Cons price for asphalt patch was $40.00 per ton and there was 110 tons Malone Drainage Overview page 2 remaining. The Street Department purchases Type D asphalt at $19.50 a ton. This allowed us to place 225 tons of asphalt on Gober instead of 110 tons. Additional savings to us were realized by not bearing the cost of cement stabilizing the subgrade since Tri-Con provided all material, equipment, and labor. Item SP.4 was for lowering waterlines where it was in conflict with the storm drain. The plans identified these locations and specified to lower or encase. We did not have a price for encasement which would be cheaper than the cost of lowering the waterline. The contractor gave us a price of $500 for each encasement and the price for lowering was $1,000. We encased 5 waterlines instead of lowering them saving $2,500 overall. Our specifications require that sanitary sewer when placed inside a junction box must be replaced with ductile iron pipe. There were three locations that required this and we did not have a price for 6" or 8" ductile iron pipe. Upon request, the contractor gave us prices of $30 a foot for 6" and $35 a foot for 8" This increased the cost $950. Total overages equal $17,199.40 or 3.8%. The following is a break down of over and under by line item. ITEM DESCRIPTION OVERAGES REDUCTIONS SP-10 Rock Excavation $12,984.00 3-A Remove Concrete Pavement $ 60.00 8o2-A Concrete Curb & Gutter 3,060.00 5.8A 6" Concrete FLT Wk 120.00 8.3A 4" Concrete Sidewalk 1,152.90 8o3B 6" Concrete Driveway 1,850.00 SP.4 Lower Waterlines 5,000.00 2.12.3A 18" RCP Class III 600.00 2.12.30 24" RCP Class III 800.00 3.9 Sod 82.50 EXTRA Concrete Encase Waterline 2,500.00 EXTRA 6" Ductile Iron Pipe 600.00 EXTRA 8" Ductile Iron Pipe 350.00 TOTAL $23,179.40 $ 5,980.00 There has been at least two heavy rains since construction was completed and this system functioned.very well. We are submitting Change Order #1 for the additional work completed. Please submit to City Council for approval and final acceptance. If you need further information, please advise. Rog0r McDaniel -- 0835E